However, I don't have surface for checking the plane of the ways to ensure it's not warped - meaning I thought I didn't have the tools to do it. So, I improvised. The next best thing was sitting in a gun case.... I had one of those laser sighting tools that sits in the chamber. I grabbed that, threw it into the drill chuck on the headstock, and slowly adjusted it until I had it spinning without any run out (I hand turned the spindle - I didn't want it too fast).
I aligned the tailstock with the laser, and then adjusted the extension on the tailstock to make sure it was lined up. It looked great. I slid the tailstock back a little bit, and checked it again. I repeated this process multiple times until the last 4" of the ways - and saw some drift. There was some slight warping from the heating. I should have used a scraper to remove the warp, but I instead used a bastard file. It took a couple of runs at it before it brought it back in line (it was about 0.05" off). I am now the proud owner of a completely operational 534.0601 wood lathe with the metal turning attachment.
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